Having completed the model Trevithick dredger engine, and not having an inspiration to start another major build, I decided to make another steam driven boiler feed pump.
Earlier this year (2019) I made a horizontal, duplex, twin cylinder feed pump for the 6″ vertical boiler, but I had also purchased the castings and plans for a vertical, single cylinder feed pump, not having decided which version to fit to the boiler. The horizontal twin version fits and functions very well, but I decided to make the vertical version while I am thinking about another major build.
So over the past few days, excluding the ones over 38ºc (100ºf), I have been machining the gun metal castings. And making a real mess of it.
- The steam cylinder bore. Bored with a boring head on the milling machine. Turned out nicely, but I decided to run a 3/4″ reamer while it was set up on the mill, thinking that the dimension would be more accurate. I did not notice until too late that the reamer was damaged. It badly scored the bore. I considered making a new cylinder from bar stock, but used the boring head to remove the scores. Now 0.75mm oversize. Annoying but not fatal.
- Steam passage not centered.
3. This one could have been fatal. All of the center drill holes for the screws and steam passages in the cylinder valve face were off by about 1mm. The workpiece had moved in the milling vice between setup and machining. I really thought that this would probably require a new part, but I decided to proceed and see what eventuated.
4. This was the most obvious error. Moved the mill table in the wrong direction, and the rectangular hole ended up with an extension. I don’t think that it will effect the function. And it wont be seen by anyone except me, and all of you blog readers. Oh, and now I have to kill you.
5. This was another mill problem. I had changed the tools to a 1.6mm drill bit, and reset the Z axis zero. Or had I? Maybe I had neglected to hit <enter> after the reset. Anyway, the chuck crashed at high speed into the job, impaling and snapping off the drill bit, gouging the steam chest, and the drill chuck gouged the milling vice. The chuck survived but required some remodelling on the belt sander and then a diamond file. The vice jaw also needed some impact craters to be flattened, then swapped out to another less critical vice.
There were some other more minor issues, which do not bear repeating and prolonging this missive. This all happened over 2 days. Mistakes are made, and I console myself with my father’s advice “he who makes no mistakes makes nothing”. But, this is the worst run of blues which I can remember. It IS hot, which is not ideal machining conditions. So what do I do?
Well, maybe it is just a bad patch, and things will be better next session. And, I will try to be not SO impatient to get things finished that I don’t double check. I (and you) will just have to wait and see.
BTW, have a safe and happy new year. 2020. It is 101 years since we had a double number year (1919), and most of us will not see the next one (2121). So make the most of it!